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OVERHAUL 2015 - 2022


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In April 2022 Sir Nigel Gresley returned from an overhaul which took more than six years and cost about £800,000 plus about £100,000 for the support coach. If you would like to make a donation towards the cost of this overhaul please click on the donate button.


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Notes from information supplied by Darrin Crone, Locomotive Engineer.

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April to June 2017.

25 June 2017

The safety valves have now been inspected, reassembled and returned to store.

The superheater header end plugs were removed this week. They allow access for expanding the outer rows of superheater elements into the header. The plugs were seal welded in and drilling through them started last week. This was continued this week and the rest were drilled through, then using the oxy-burning gear the plugs were burnt out. The holes have been enlarged over the years to repair the threads for the plugs and they are now too large to repair in the same way, so now new material will have to be added and the holes remade.

The air pump governor was reassembled with new seals this week. It will not be fitted to the loco yet as we plan to reposition it to improve its accessibility in traffic.

The wasted studs have now been removed from the regulator stuffing box. Not an easy job to do when the studs are of steel in a bronze casting. As the studs are harder than the bronze it is very easy to damage the stuffing box casting. The studs that fasten the side gland followers have also been removed and the casting and cover have been cleaned to enable a closer inspection.

We have decided to replace our clackboxes. They have given us good service and look to be originals but they are showing signs of wear and do carry evidence of previous repairs. This week I collected the patterns from their owners and transport to the foundry is now being organised.

On the loco frames spotfacing continued on the combined spring and brakeshaft bracket, with another hole completed and a further hole prepared for a final cut. This will be the last hole requiring spotfacing. Up in the saddle the Engineering Team has been patiently working on the bolt holes used to fasten the saddle and middle cylinder castings together. Progress has been frustratingly slow as scale and corrosion has had to be removed from the hidden lower face to allow clearance for an adequate bolting face.

Undercoat was applied to the outside of the frames this week in preparation for applying gloss. The reverser shaft is now also finish painted and painting is continuing on the underside of the footplating.

Bob Shearman casts a critical eye over the technique of Darrin crone as he removes the superheater plugs. 20 June 2017
Photograph: Peter Brackstone.

Removing superheater plugs

The outside of the loco frames are now receiving undercoat. 22 June 2017
Photograph: Peter Brackstone.

Undercoating loco frames

Peter Brackstone rubs down undercoat on the left side of the frames in preparation for another coat of paint on 22 June 2017
Photograph: Darrin Crone.

Prepping left side of the frames

Tony Bickerstaffe prepares the last hole for spotfacing on the right hand leading combined brake and spring bracket on 22 June 2017
Photograph: Darrin Crone.

Last hole for spotfacing

The spotfaced bracket. The lower two holes require countersinking. 22 June 2017
Photograph: Darrin Crone.

Spotfaced bracket

The superheater header has had the end plugs removed. It is now ready to go to contractors for repair. 22 June 2017
Photograph: Darrin Crone.

Superheater header

The regulator stuffing box has had all its studs removed and will now be closely inspected. The large flange on top is fastened vertically to the boiler backhead. The gland hole accepts the regulator cross shaft in the cab and is at the lower end. 22 June 2017
Photograph: Darrin Crone.

Regulator stuffing box

The regulator cross shaft is pinned to the regulator reach rod. The pin is kept in place by the stuffing box cover and the head of the pin runs on a pad cast on the cover. 22 June 2017
Photograph: Darrin Crone.

Regulator cross shaft

The air pump governor is now completed. The governor regulates the steam pressure going to the pump which in turn determines the pressure of the air the pump generates. 22 June 2017
Photograph: Darrin Crone.

Air pump governor

18 June 2017

On Tuesday the air brake components, voltage regulator and dynamo removed from the coach were collected by Rampart, our coach chassis overhaul contractors. It is planned that the coach will follow in early July. The air brake distributor mounting manifold and the fittings recovered from the other air brake components were refitted to the coach and were sealed with duct tape.

The loco brakeshafts were dye penetrant inspected this week and no faults were found.

We have now received the final documentation for the new copper tubeplate so it can leave Crewe. Llangollen Railway Engineering is now organising collection and delivery to its works. At Llangollen the stays have been removed from the throat plate and backhead where sections of plate above the foundation ring was found to be grooved and was removed. The steam supply pipe from the backhead to the internal manifold has also been removed to repair the joint in the backhead pad. This had been a source of problems in the past so the joint will be refurbished. The combustion chamber and back corner stays we decided to renew at this overhaul have now all been removed and the holes will now be reamed.

Work continues on the loco bogie stretcher with removal of the loco bogie side bearers that stop excessive rolling of the loco. The side bearers are in need of refurbishment and will require new bolts. The cleaning of the underneath of the stretcher continued this week and was completed after some needle gunning under the left hand cylinder before the Painting Team were sufficiently satisfied with the level of cleanliness. The top of the stretcher also saw the needle gun this week and the final traces of scale being removed.

Above the loco bogie stretcher work continues on the bolt holes that go through the saddle and middle cylinder. The top of the the holes are finished but the bottoms, hidden under a flange require attention. We need to spotface these holes however the location and proximity to the side of the casting is giving us problems.

Areas receiving top coats of paint this week included inside the space between the front bufferbeam and cylinders. The reversing shaft is now up to undercoat.

The air pump reassembly continued this week with the addition of the high pressure air cylinder and end covers. The pump was laid on the surface table so that the mounting brackets on the steam cylinder and low pressure air cylinder could be accurately aligned. The air pump was lifted in to position on Thursday and fits very well on to the mounting plate in the frames without the use of shims previously used under the mounting brackets.

The air pump steam inlet flange required new studs and these we made and fitted this week. An order has been placed for new loco and bogie spring hanger bolts and material has now arrived at our contractors and we have received the material certification.

The outside crankpins in our centre coupled wheels have now been removed at Buckfastliegh. The wheelset has been put on the "quartering" machine and the machining of the crankpin holes is underway. The material for the crankpins has been cut and machining of the pins has started.

The safety valves have now been stripped and inspected. The rear valve sees little use as the leading valve is set to blow at a lower pressure. As the leading valve does by far the most work it has worn and we think it's time to replace it. The trailing valve, apart from some external marking, is in very good condition, though will require a new spring.

The hose connectors to the leading vacuum cylinders were retrieved from store this week and trial fitted to the cylinders. When tried in place it was found that their mounting flanges were not flat, probably from being clamped on to thick soft seals. They were skillfully hand fitted this week and they are now sit flat on to the cylinders.

Another part retrieved from store and receiving attention is the regulator stuffing box which sits on the boiler backhead in the cab. It takes the shaft that runs between the regulator handles and encloses the joint between the shaft and the rod that goes in to the boiler to the regulator valve. A start has been made on the removal of the life expired studs.

The final journal centre dimensions have been taken from the coupled wheel axleboxes. All six boxes have been done so that they can now be transported to our contractors for remetalling.

We plan to dispatch the superheater header for refurbishment on the road transport that returns our pistons. We have carried out some work on the header, as the more we do using the Engineering Team the less there will be for the contractor, and this will reduce the cost. This week we began to remove the seal welded plugs in the ends of the header. The plugs give access to enable expanding the outer rows of superheater element tubes. The Engineering Team started the removal by drilling through the plug centres.

The left loco bogie side bearer bolted through the bogie stretcher, frames and outside cylinder. A view from the inside looking on the bogie stretcher flange. 13 June 2017
Photograph: Darrin Crone.

The left loco bogie side bearer

The leading brake shaft was put up on a trestle for di-pen inspection. 13 June 2017
Photograph: Darrin Crone.

The leading brake shaft

The air pump was put up on the surface table in the NRM Workshop to ensure it would fit flat on the loco mounting plate. Roger Turnbull checks for tightness in the bolted joints before fitting to the loco. 13 June 2017
Photograph: Darrin Crone.

The air pump

The air pump in position on the loco frames on 15 June 2017.
Photograph: Peter Brackston.

The air pump in position

The front safety valve laid out for inspection on 16 June 2017. It shows erosion in the bottom flange and in thetop cover where steam at 250 pounds per square inch ferociously rushes through when it blows.
Photograph: Darrin Crone.

The front safety valve

The end plugs in the superheater header are in the process of being drilled through. 16 June 2017
Photograph: Darrin Crone.

Superheater header plug

One of the vacuum brake cylinder connectors. It has been cleaned and dressed with the attachment flange flattened to provide a good seal on the cylinder. 16 June 2017
Photograph: Darrin Crone.

Vacuum brake cylinder

Not mentioned in the text, one of the leading vacuum brake cylinders on the NRM Workshop Union borer. The trunnions show wear and are to be skimmed and re-sleeved. We have LNER/BR documentation showing this permitted repair procedure. 16 June 2017
Photograph: Darrin Crone.

Vacuum brake cylinder

11 June 2017

The steam cylinder off the air pump was finish machined last week but the bore still needed to be cleaned, so it was polished and honed this week and reassembled to the low pressure air cylinder with the piston rod and pistons in place. The rod that controls the admission of steam to either side of the steam piston was trial fitted with the top end cover in place to check the travel of the pistons and rod. All seems to be in order.

Last week a start was made on the spotfacing of the right hand leading combined brake shaft and spring bracket mounting holes using burrs to remove the first material. This week the the spotfacing tool was applied and two holes were finished.

Cleaning of the coach dynamo continued this week. The BR instruction says that it should be wire brushed and another coat of bitumen applied. Having been subject to this regime the coating was coming off in thick pieces with the surface of the dynamo showing surface corrosion, so it was decided to take it back to a sound surface and give it a coat of primer. We didn't want to apply bitumen while it has to be manipulated during overhaul and testing. This week the stripping was finished and a coat of primer applied. The seal under the domed end cover was also cleaned out so that we are sure of a good weatherproof seal.

All the parts off the coach that are going separately for overhaul have now been prepared, and collection has been organised with the contractor.

The reverser shaft key has now been repaired and fitted. It now is a good fit in both the shaft and the reverser lock sheaves. The special eyebolt that fastens the reverser spring to the vacuum clutch frame stretcher has now been refurbished. The reverser spring is fractured so a new one is needed. A number of specialist spring manufactures has been contacted and quotes are awaited.

At Llangollen we had a very productive meeting with our insurers, the body responsible for our mainline certification and Llangollen engineering. The method of preparation for the fitting of the new tubeplate has been agreed which involves the refurbishment of the combustion chamber plates. We also measured the combustion chamber opening to assess how much distortion, and therefore the amount of movement that would be required from the plates to contact the new tubeplate. We were pleased that there is sufficient room to get the new tubeplate in comfortably without a lot of movement required from the old plates. This should give us the best possible fit.

The roof stays were also examined with our own endoscope. We had a good look round and what we saw indicated that the majority of the roof stays will be suitable for further service. However, we agreed that some stays be removed and then we will asses their condition. We also agreed that the outer rows of side stays be ultrasonically tested to ensure there are no undiscovered fractured stays in these areas.

After our visit to Llangollen we went on to Crewe to inspect the new copper firebox tubeplate. It is a very good piece of work and corresponds to drawing and our instructions issued during the placing of the contract. When we receive the final documentation for the plate we will organise transport to Llangollen.

Work between the frames on the lubrication piping continued this week with some finishing touches to the axlebox lubrication system. On Wednesday the cylinder lubrication pipework was retrieved from store. It was then flushed through and the pipes cleaned. They are now ready for annealing and fitting. Work off site on the cylinder lubricator continues.

The refurbishment of the pistons was completed this week and were inspected at our suppliers. They are now ready to be returned to York.

Work continued on the loco's bogie stretcher this week with further cleaning and the removal of most of the paint. This will allow detailed inspection. The lubrication fittings have now been removed from the stretcher and it apears that water has been passing one of the fittings. This would find its way on to the bearing surfaces between the loco and bogie. We think this explains the uneven wear we have found. The uneven wear could not be explained by uneven loading as the positions of the bearing surfaces relative to each other have been measured and all seems to be in order. We have now agreed a plan for refurbishment of the bearing surfaces.

In the Llangollen boilershop. Darrin Crone views images of the roof stays taken by the endoscope operated by Paul Aston, Engineering Team member, right. 8 June 2017
Photograph: Richard Swales.

In the Llangollen boilershop

An image taken of a roof stay by the endoscope.The thread on the end of the stay goes into the firebox crown sheet. The condition of this stay, apears to be very good and it looks to be suitable for further use, however some stays will be removed to examine their condition inside the plate. 8 June 2017
Photograph: Paul Aston.

An image taken of a roof stay

The right hand outer wrapper has now been riveted along its trailing edge to the outer doorplate. The sides are drilled to tapping size. 8 June 2017
Photograph: Richard Swales.

The right hand outer wrapper

The finished copper tubeplate at Crewe with inspection documents during final examination and acceptance by Sir Nigel Gresley Engineers. 8 June 2017
Photograph: Richard Swales.

The finished copper tubeplate

Two spotfaces were cut on the right hand combined brake shaft and spring bracket. The welds on this fabricated bracket are larger than the radius in the corners of a casting so have to be cut in to to provide a clamping face for the bolt that will be fitted in to the hole. 10 June 2017
Photograph: Richard Swales.

Brake shaft and spring bracket

Not mentioned in the report, the coupled wheel axle boxes are being put on the marking out table at the NRM, York. The disc in the centre is exactly the same size as the axle journal that runs in this bearing. Measuring from the centre of the disc allows the position of the axle on the locomotive to be calculated. This is important as when the axleboxes are re-metaled the centre dimensions will need to be known accurately. 10 June 2017
Photograph: Richard Swales.

Coupled wheel axle boxes

Not mentioned in the report, the safety valves were retrieved from store this week. They will be stripped and examined for condition. 10 June 2017
Photograph: Darrin Crone.

Safety valves

The underneath of the loco bogie stretcher now cleaned, though a little work is left to do. 10 June 2017
Photograph: Darrin Crone.

Loco bogie stretcher

The major components of the air pump is now being reassembled, the steam cylinder to the right and the low pressure air cylinder to the left. 10 June 2017
Photograph: Darrin Crone.

Components of the air pump

4 June 2017

The overhauled vacuum clutch that holds the reverser shaft was refitted to the loco this week, and the remaining pipework refitted, so the compete pipework from clutch to the Cartazzi frames is now in place. The fit of the clutch sheaves on the shaft has been checked. To ensure no movement on the shaft the sheaves are keyed and we thought the fit could be improved so the key was rebuilt and will be tightly fitted in to the shaft.

The air pump governor was retrieved from store this week and its overhaul has began. The repaired air pump steam cylinder end flanges have now been faced and the flange holes drilled and tapped where the cylinder was welded. The cylinder bore requires polishing and then the pump will be ready for reassembly.

The pistons are now in the process of repair with the left completed and the right, by the end of the week, on the lathe at the works of K D Flavell with the ring grooves being machined. At Llangollen the roof stays have been examined more closely now that the sling stays have been removed. It apears that the main body of roof stays are in good condition and it may be possible to retain these. The outer wrapper plate on the left has now received its final adjustments and has been finally fitted in place. The plate on the right side has now been offered up and tack welded in position. On the South Devon Railway the wheelset re-tyring has now been completed. As the refurbishment of the wheelsets has been straight forward and has not incurred any substantial unexpected expense it has been decided to replace the driving crankpins on the crank axle. We knew they were getting toward minimum size but wear on them is very slow over time, however as insurance against having to skim them below scrapping size during the next period in traffic, and the possible time out of service that would result in, we have decided to replace them now.

The spotfacing of the top of the bolt holes between the saddle and middle cylinders was completed this week. We are now considering ways of spotfacing the other end of the bolt holes. The outside cylinder flange holes received their final honing this week and a start made on spotfacing and countersinking the holes in the back of the recently replaced combined brake and spring bracket.

From the public's point of view the biggest change in the workshop this week was the shunting of the tender to next to the loco. On Tuesday afternoon we cleared the last of our components from the space needed for the tender and refitted the drawbar so that the tender could be shunted. The shunt was completed after the museum closed with the Engineering Team shunting Rocket by hand while the NRM diesel shunter moved our tender. Next day the draw bar components were removed from the tender.

This week the Engineering Team began the overhaul of the support coach and started by removing the air brake components that we will be sending away for overhaul. On Thursday all the air brake components we need off the coach were removed, including both air brake cylinders, auxiliary reservoir tank, strainer check valve unit and distributor. We are also refurbishing the dynamo and voltage regulator and these have also now been removed. The removed air brake parts have been put on pallets and will be collected by contractors. The dynamo has been cleaned and stripped, though there is more work to be done on this.

The loco's bogie stretcher had another shift of cleaning, but there is more to do yet. The bogie and the bogie centre casting have received detailed inspection this week. The centre casting was put up on the workshop marking out table and then measured.

The air pump steam cylinder has had the end flanges and lead in to the bore re-machined. Holes at either end, filled with weld required drilling and tapping. This was done on the NRM's Richmond radial arm drill. 3 June 2017.
Photograph: Darrin Crone.

Air pump steam cylinder

Not mentioned in the report, painting has continued around the loco. Here the underneath of the right hand footplating is receiving coats of undercoat. 3 June 2017.
Photograph: Darrin Crone.

Painting has continued

The tender is now next to the loco, at the buffers so will not be in the way of future shunts in the workshop. As we don't now have to keep the tender mobile it's overhaul can now start in earnest. 3 June 2017.
Photograph: Darrin Crone.

Tender is now next to the loco

The bogie centre casting has a number of bearing surfaces that require measuring for flatness, height and squareness. It has been put up on the marking out table in the NRM workshop so that this process can be carried out accurately. 3 June 2017.
Photograph: Darrin Crone.

Bogie centre casting

The coach dynamo was removed and is in the process of getting a good clean. 3 June 2017.
Photograph: Darrin Crone.

The coach dynamo

The top of the middle cylinder and saddle bolt holes at the rear of the saddle have been spotfaced to ensure a good long term bolted joint 3 June 2017..
Photograph: Darrin Crone.

The top of the middle cylinder

The vacuum clutch refitted to the loco. 3 June 2017.
Photograph: Darrin Crone.

The vacuum clutch refitted

The clutch grips the reverser shaft by closing on to the sheaves shown in the picture. To ensure the sheaves don't rotate on the shaft they are keyed. The key is shown protruding against the shaft. 3 June 2017.
Photograph: Darrin Crone.

Clutch grips the reverser shaft

The right hand piston head has been built up with weld and is on a Dean, Smith and Grace lathe at the works of K D Flavell to be machined truly round and to size. 3 June 2017.
Photograph: Darrin Crone.

The right hand piston head

20 May 2017

We started the week with the lifting of the loco and the removal of the accommodation bogie. It had been planned to move the bogie clear of the front of the frames, however we finally decided to move the bogie in to the trailing bogie wheel cut out in the frames, just to the rear of the cylinders. This meant that we didn't have to lift the frames so high, we don't use up valuable space in front of the loco and when packing is added to the top of the accommodation bogie it will act as an additional support. The available space was measured to make sure it would fit and it would not hinder work on the frames. So the team lifted the engine using jacks on the front bufferbeam while ensuring we had a level lift, and followed the lift with the screw jacks. When lifted sufficiently high to clear the spigot on the loco's bogie stretcher the bogie was pushed back and then the loco was lowered and the frames levelled.

We can now access the bogie stretcher all round so cleaning has begun. There is still some time to be spent on this then the paint will be striped off and the stretcher will be examined. The stretcher does not only load the bogie but also ties the outside cylinders and frames together.

Painting continued on the loco bogie with top coats now being applied and the expansion link brackets received their first top coats. We are painting these brackets as when the reversing shaft is refitted they won't be so accessible. The reversing shaft has now been thoroughly cleaned with all paint removed by needle gun. The end threads and key ways were degreased and di-pen inspection has now been completed. After painting the shaft will be ready for reuse. The brake shafts have also now been finish cleaned and await inspection. The loco brake hangers were also removed from the loco after trial fitting and have been cleaned and needle gunned prior to refurbishment.

The new seals for the brake cylinders have arrived and await refitting. The seals under the piston rod cover plates were replaced this week. The leading cylinder mounting brackets were retrieved from store and their fit on the leading cylinder mounting trunnions examined. There is noticeable heavy wear on the trunnions and the centre bracket which will require repair.

New cylinder cover studs were fitted to the middle cylinder this week, the old ones being removed as life expired. Some of these studs go in to steam spaces so they were sealed in. All studs now run out of thread on their shanks as previously some of the old ones bottomed out.

Work on the refurbished combined brake and spring bracket continued with reaming of the fixing holes. All holes have now seen the reamer, though a couple still need some further work. A plan for spotfacing and countersinking the back of the bracket has been devised and tooling is now being sought.

The boring of the leading top cylinder mounting holes has been completed and the last two holes that could not be accessed by a reamer have been honed. The job has now been reviewed and impressed by the honed finish it has been decided that another day should be spent with the hone to clean up the other holes then they will be measured for new fitted bolts.

The last axlebox hard pipe was annealed and fitted this week and work then moved on to start the refurbishment and refitting of the vacuum clutch pipework.

Progress on the boiler at Llangollen has now started with the removal of stays in the back corners of the firebox. They have not caused us any problems but are to be replaced as a precautionary measure due to age and they are known to be in a stressed area. The leading, sling stays that support the firebox crown have been removed to enable the new tubeplate to be fitted. The new tubeplate is now complete and is ready for our inspection at LNWR Crewe.

The loco frames are being lifted to allow the removal of the accommodation bogie that has been supporting the front end. Bob Shearman operates the jack while Andy Barwick checks to see the gap between the loco and the accommodation bogie on 16 May 2017.
Photograph: Darrin Crone.

Loco frames are being lifted

With the accommodation bogie removed we now have access to the bottom of the loco bogie stretcher and pivot. 16 May 2017.
Photograph: Darrin Crone.

Accommodation bogie removed

The front of the frames are now supported by screw jacks. 16 May 2017.
Photograph: Darrin Crone.

Screw jacks supporting frames

With the accommodation bogie removed the bolts that run through the bogie stretcher, frames and outside cylinders can be accessed. The right hand cylinder is the only one marked LNE and may be the original fitted at Doncaster during construction. 16 May 2017.
Photograph: Darrin Crone.

R/H cylinder marked LNE

The reverser shaft is marked with Sir Nigel Gresley's original LNER number 4498. 16 May 2017.
Photograph: Darrin Crone.

Reverser shaft marked 4498

Not something you see every day, a view up the middle of the bogie pivot in the loco stretcher. The pin is keyed in to the top of the hole. The pin was removed last week. 16 May 2017.
Photograph: Darrin Crone.

Middle of the bogie pivot

Inside the boiler the sling stays are being removed. This will allow the crown plate flexibility to enable the fitting of the new tubeplate. 18 May 2017.
Photograph: Paul Aston.

Sling stays are being removed

The inspection of the reverser shaft has now been completed. 19 May 2017.
Photograph: Darrin Crone.

Reverser shaft

The loco brake hangers have been trial fitted and show wear that will have to be repaired. Prior to this work they are being needle gunned by Peter James to remove old paint so that any hidden faults can be found. 19 May 2017.
Photograph: Darrin Crone.

Loco brake hangers

14 May 2017

The reverser clutch has been under overhaul over the last few weeks and has received new brake linings. This week we received the new rubber diaphragm. To keep production costs down the diaphragms are supplied without holes so these have to be punched through. This was done and then the clutch was reassembled. It can now be refitted to the loco. A spare diaphragm was also obtained and this has also been punched and it will be put in store.

The clutch grips on to the reversing shaft. The shaft was put up on trestles this week and removal of the paint and general cleaning was began prior to inspection. The end journals were inspected and are round and parallel and show little wear. The bearings in the brackets on the loco were also inspected. These are in a satisfactory condition and will not require replacement.

The regulator valve overhaul continued this week with the valve seat lapped using a special tool brought from our Grosmont store. The valve and pilot valve were both skimmed by Danny Holmes of the NRM to restore their faces, the pilot valve showing the most wear. The pilot valve was then used to lap the pilot seat in the top of the regulator valve. Inside the valve there are rings that run in an internal bore. This bore was cleaned and the unit reassembled. On the bench the travel of the valve was measured and compared to the LNER drawing. The movement of the operating lever connected to the regulator lever in the cab, was confirmed to produce the correct lift of the regulator valve. During the valve rebuild the brackets that support the valve in the boiler and the operating half shafts were di-pin inspected and no defects were found. New bolting is required then the regulator valve overhaul is complete and it can be refitted to the boiler.

Painting this week continued on the loco frames inside, behind the bufferbeam, and on the bogie. The cylinder ends received their first coats of high temperature black. The bogie by the end of the week was receiving undercoat. Before painting began on the top of the bogie Alan Pitt di-pen inspected the welds around the sections added to the bogie centre casting and to an old weld repair. No faults were found.

The bogie centre casting that sits between the bogie stretcher on the loco and the centre casting in the bogie frames received di-pen inspection this week. There is more to do on this item and it will need a comprehensive dimensional inspection to determain why it shows uneven wear. Our CME completed his dimension inspection of the bogie frames this week.

The position of the refurbished combined spring and brake shaft bracket was confirmed on Tuesday, just to make sure before new fixing holes were drilled through. After last week's disappointment with the breaking of the cutter on the first hole it was not without trepidation that the mag-drill was started and the cutter entered its first hole. However the drilling went well and the same cutter managed to drill all the fitted bolt holes. In addition to the bolt holes there are two smaller sized rivet holes that were drilled through in stages using standard drills. Four of the old fitted bolts were machined as clearance bolts and have been used to clamp the bracket in place. The bolt holes will need reaming and new bolts making, but before this the back of the bracket will require countersinking for the rivets and spotfacing for bolting where the holes are near to the welds.

The loco brake shafts, of which there are two, were moved to near the bogie for inspection and refurbishment. Whilst taking the paint off the trailing shaft it was discovered that it is marked 4901. There was an A4 numbered 4901 and named Capercaillie, which became BR 60005 Sir Charles Newton.

Reinstalling pipework between the frames continued this week with the refitting the couplings that connect the axlebox lubrication hard pipes to the hoses that are connected to the coupled wheel axlebox underkeeps. The steam sands steam supply pipe was cleaned, annealed and refitted between the tee on the stretcher between the sand boxes and the Cartazzi frames. The pipes to the vacuum clutch were also retrieved from store this week and the last remaining copper pipe for the axlebox lubrication system. Cleaning and annealing of these pipes has begun.

The boring of the cylinder mounting holes continued this week but as the job gets harder the progress slows. After a number of modifications to the jig the last and most inaccessible hole has been bored through. Before work stopped last Thursday the last finishing cut was just short of breaking through.

We are planning to remove the accommodation bogie and support the front of the loco frames on our new screw jacks. This will enable the loco bogie stretcher and lower outside cylinder bolts and studs to be examined. To use the jacks we need a beam for them to stand on as we are over a pit and the distance over the frames is within rail gauge. We were given surplus steel beam by Simon Holroyd and two lengths were cut to size. Some steel packing was required to make them level with the rail head and this was cut to size, and then the assembly was welded together. After grinding to ensure a good fit between the rails the beam assembly was lowered in to position with the crane. The jacks were then put in position ready for the lift. The bogie pivot pin was also removed so that the frames don't have to be lifted so high to clear the accommodation bogie.

The valve chests that require new liners have now been measured by the supplier and the liners will now be finish machined. When they are finished, fitting will be organised.

The top of the bogie centre casting that slides from side to side in the bogie. The loco pivot pin goes down the centre hole. 9 May 2017
Photograph: Darrin Crone.

Bogie centre casting

The holes for the mounting of the leading right hand combined brakeshaft and spring bracket were drilled through this week. Malcom Bateman supervises as John Livesey feeds in the cutter. 10 May 2017
Photograph: Darrin Crone.

Holes drilled through

The bogie pivot pin was removed this week. The nut is at the lower end of the pin. 13 May 2017
Photograph: Darrin Crone.

The bogie pivot pin

Not mentioned in the report but a new, special thread stud had to be manufactured for the manifold. This is shown fitted in the centre top hole. The manifold shut off valve has been repacked and the overhaul of this assembly is now complete. 13 May 2017
Photograph: Darrin Crone.

New special thread stud

The screw jacks under the front of the loco frames will take the weight of the frames when the accommodation bogie is removed. 13 May 2017
Photograph: Darrin Crone.

The screw jacks

The loco brake shafts are now being refurbished. The trailing shaft has the long arm laying on top of the leading shaft. 13 May 2017
Photograph: Darrin Crone.

The loco brake shafts

The long arm on the trailing shaft is marked 4901. 13 May 2017
Photograph: Darrin Crone.

Long arm marked 4901

7 May 2017

The bogie side control springs were fitted this week. When in position they are compressed to a load of 4 tons and they need to be compressed more than this to get them in to the bogie. A spring compressor was made by the NRM for doing this job and they allowed us to use it. So after some hard work both springs were refitted. With the springs in place and the bottom of the bogie painting completed we could then turn it over. To give us a bit more room we decided that we needed to move Rocket's boiler. With the permission of Simon Holroyd the workshop manager we lifted the boiler on to the wheel drop. Then on forklift trucks we moved the bogie under the crane and turned the bogie over. Once the right way up we put the bogie back where it has been, behind our tender, then put Rocket's boiler back.

With the bogie righted, work began on preparing the top surfaces for inspection and painting. The separate bogie centre casting that accepts the pivot pin fixed on the loco was retrieved and inspection of this item has began.

Inspection and refurbishment of loco and boiler fittings is now well under way and continued this week with the regulator valve put up on the bench and stripped down. After spending ten years in the boiler it was reluctant to come apart but by the end of the week we had got the valve in to its components parts. The valve was inspected and it apears to be in good condition. Down stream of the regulator in the smokebox are the steel, main steam pipes and these have been inspected for thickness. They have now been approved for continued use.

Work on the manifold continued this week with the copper seal between the manifold shut off valve and the manifold body being annealed and refitted. The stuffing box was repacked and it has been reassembled in to the manifold. The new diaphragm for the reverser vacuum clutch was delivered this week. The diaphragm holes were punched through and then trial reassembled in the clutch. The repaired air pump steam cylinder was also returned this week.

Painting continued this week with gloss applied to the front sections of the Cartazzi frame by the Painting Team. Painting also continued inside the front section of frames behind the bufferbeam.

Work continued on the bolt holes between the rear flange of the saddle casting and middle cylinder. The holes were cleaned up by drilling through and reaming to produce a consistent hole diameter. We need this so that we can use our spotfacing tool. On Saturday work continued with the spotfacer and the first hole was completed and is now ready for bolting.

The boring of the cylinder flange holes continued this week with the penultimate hole bored. This is by far the most difficult hole to get in to and it has required a number of modifications to the alignment jig. As it is too tight to get a reamer in to finish the hole it is planned to finish the hole by honing.

The final fitted bolt was fitted to the horn castings this week to the leading side of the right driving horn. To get the nut and spanner on the new bolt 2 of the vertical hornstay bolts had to be removed. After torquing the new bolt the hornstay bolts were refitted.

The brake hangers were trial mounted on the loco some time ago for inspection and this has now been done. The hangers have worn where they carry the brake blocks. As the brake hangers wear and the clearance between hanger and brake block increases the brake block position is not controlled as well as it should be, and due to the slope of the tyre profile the brake block begins to contact the tyre further to the outside of the wheel. This wear is to be expected and some do show signs of being rebuild with weld in the past. It is now necessary to rebuild the hangers again. The trailing two hangers were removed on Saturday by the 007 Gang, our junior volunteers and were given a clean and needle gunned in preparation for repair.

The rebuilt combined right hand leading spring and brake shaft bracket was refitted this week. The fit of the bracket was improved by further dressing of the frame bottom to match the flatness of the machined surface on the bracket. When finally positioned it was clamped in place and held by jacks. It was then planned to drill through a couple of holes and bolt through to fix its location, however the hole cutter broke on the first hole, so we will have to get a new cutter and try again.

The screw jacks given to us last week were brought in and were stripped and inspected. They are in good condition and have now been prime painted. As soon as they are finished they will be used to support the front of the loco and the accommodation bogie will be removed.

The first of the side control springs refitted in the bogie. 2 May 2017
Photograph: Darrin Crone.

Side control springs

John Livesey drills through the bolt holes between the saddle and middle cylinder flange while Peter Brackstone paints between the frames on 3 May 2017.
Photograph: Darrin Crone.

Peter Brackstone painting

Tony Bickerstaffe boring the saddle and cylinder flange holes on 4 May 2017.
Photograph: Darrin Crone.

Tony Bickerstaffe boring

We have shared the workshop this week with sister A4 60009 Union of South Africa. 4 May 2017
Photograph: Ken Woods.

60009 Union of South Africa

The right hand leading combined spring and brake shaft bracket in position on the loco frames on 6 May 2017.
Photograph: Darrin Crone.

Spring & brake shaft bracket

Our new screw jacks are being given a coat of paint before being put in to service. The body castings are on the floor while the screws are on the bench on 6 May 2017.
Photograph: Darrin Crone.

Our new screw jacks

The bogie now right way up and put back behind our tender on 6 May 2017.
Photograph: Darrin Crone.

Bogie now right way up

1 May 2017

The coupled wheel springs, secured to pallets, were moved to the workshop doors to be collected on Tuesday. However the carrier turned up a day late and collected on Wednesday. Fortunately Simon Holroyd was around and drove the forklift and skillfully got them in to the rather small van that turned up to collect them. We had been expecting a truck. They are now gone for contractor refurbishment.

We were offered some surplus screw jacks that we can stand the frames on. These were retrieved from a North Yorkshire location this week. I believe they needed cutting out of the undergrowth, so thanks to the dedicated Engineering Team volunteers who rescued them. However, we will need to clean them up and assess their condition before we can use them. We need additional jacks to support the front of the loco when we remove the accommodation bogie so that we can work on the bogie stretcher and lower outside cylinder flanges.

The brackets that carry the unions between the copper pipe and axlebox flexible lubrication pipes were fitted to the frames this week. They have been painted in undercoat and will be glossed whist on the frames. Painting of various brackets has continued inside the frames.

Painting continued on the bogie this week with undercoating completed on the underside of the bogie. By the end of the week the underside of the bogie had been finish glossed and now awaits the fitting of the side control springs. It will then be turned back the right way up.

Removal of the paint from the Cartazzi axle continued this week and by the end of the week it had been given a couple of coats of primer. Undercoat has now been applied to the front sections of the Cartazzi frames.

The manifold overhaul continued this week with di-pen inspection and the refurbishment of the manifold shut off valve. The faces that the manifold valves seat on were quite marked so these have now been carefully dressed and the marking removed. Di-pen inspection was also carried out on some of the draw gear components this week. The front hook, intermediate drawbar, tender eyebolt and main loco pin were completed.

The right hand combined brake shaft and spring bracket was set up on the horizontal borer this week and the trailing edge skimmed where it was fouling the hornstay when trial fitted. The newly machined section was deburred and the bottom of the frame where the bracket fits dressed, as there was still some traces of old weld. The edge of the frame was chamfered to ensure that the bracket will fit tight to the frame.

The mechanical lubricator returned to York last week was fitted this week and progress was made in the refitting of the lubrication pipe work to the axleboxes.

A new fitted bolt is required for one of the right hand horn castings, however as with the other loose bolts we have found in the horns the face under the nut is poor. So this week the hole was spot faced until a continuous face was produced. A good result was finally produced. Work also continued this week on the cylinder flange holes with only 1 hole finished this week. This was reamed out and a start was made on the boring of one of the final two holes.

The vacuum brake cylinders components were laid out this week for further cleaning and inspection. Some of the parts where fit is important have now been measured and the piston rods were di-penned.

The combined brake and spring bracket revisits the NRM's Union horizontal borer for the edge to be machined back. 25 April 2017
Photograph: Darrin Crone.

Brake and spring bracket

The manifold with wasted studs removed has been dye penetrant tested to examine for cracks and flaws. 25 April 2017
Photograph: Darrin Crone.

Manifold without wasted studs

The draw gear components are being inspected for wear and damage. This is the front loco hook. 26 April 2017
Photograph: Darrin Crone.

The draw gear components

The Cartazzi axle has been stripped and primed. 26 April 2017
Photograph: Peter Brackstone.

The Cartazzi axle

The paint on the frames is now extending on to the Cartazzi frame extensions as Roger Turnbull fits lubrication pipework between the frames on 27 April 2017.
Photograph: Peter Brackstone.

The paint on the frames

The last horn bolt that requires replacement has had the face on the horn casting re-cut to provide a good fastening area for the nut. 28 April 2017
Photograph: Darrin Crone.

The last horn bolt

The mechanical lubricator that supplies the axleboxes has now been refitted along with most of the pipework for the axlebox lubrication system. 28 April 2017
Photograph: Darrin Crone.

The mechanical lubricator

The mechanical lubricator can be seen on the far side of the frames and some of the pipework recently refitted. 28 April 2017
Photograph: Darrin Crone.

The mechanical lubricator

24 April 2017

With the footplate riveting finished, paint has now been applied around the riveted areas. This has enabled the two large oil boxes to the rear of the saddle casting to be fitted on freshly painted brackets. These were earlier retried from store and given a finish clean and some minor attention to the connection threads.

Earlier in the week all the axlebox mechanical lubricator copper piping was retrieved from store. The pipework, as usual, was given a further clean through and is now going through the process of inspection, repair and annealing. The Mechanical lubricator has now been returned from overhaul, which has been carried out by our CME.

The brackets that support the unions between the flexi pipes that run from the axlebox lubricator copper pipes, have been stripped down and are currently being painted. I was going to fit them to the loco and have them painted in-situ but the painting team vetoed that decision as a better job can be done on the bench. The unions themselves have received cleaning and repairs to some damaged threads.

The trial fitting of the leading right hand combined spring and brake bracket has required some dimensional investigation to ensure that when left and right brakeshaft bearings are placed on the same centre line that the right hand bracket positions the centre of the spring under the centre of the axlebox. In addition we have to ensure that there is sufficient clearance for the spring to move while in traffic. To achieve the common bearing centre line still requires the removal of some material from the trailing edge of the bracket for final fitting as when trialed it was very near the hornstay.

Work on the manifold assembly continued this week with attention turning to the manifold casting itself. All the valves have now been refurbished except for the manifold shut off valve which is an integral part of the manifold casting. Work started by removing wasted studs, then cleaning and carefully abrasive blasting the surface. This will allow a detailed inspection of the surface.

The bogie frames inspection was completed this week, and no time was wasted by the Painting Team as by the end of the week undercoat was being applied. We are concentrating on painting the underside of the bogie before we turn it back up the right way and these areas cease to be easily accessible. The side control springs, to be fitted before turning the bogie frames, were finished painted this week. The spring cups, spacers and other parts were painted some time go.

The bogie axleboxes have been closely examined and measured by our CME, however this week to ensure their soundness we di-pen inspected the flanges of the axleboxes to ensure there are no cracks. All are defect free.

Cylinder and saddle bolt boring continued this week with the boring of the first of the really challenging holes. This hole was bored through and partially reamed before work ended this week. There are only two holes left and these are the really - really challenging ones. At the trailing end of the saddle the last of the life expired bolts that fasten the saddle to the middle cylinder casting were removed this week. The holes were then cleaned out to remove corrosion.

Work began this week on the Cartazzi refurbishment with paint being removed from the wheelset axle. A bit of a challenge with it still in position the Engineering Team coped very well, as to be expected. The Team also continued the examination of the vacuum cylinders with the piston rods examined for wear and distortion. The loco drawbar gear has been removed and measured over the last few weeks and work continued this week on these parts with them receiving a good clean before they receive their crack detection examinations.

The inside of the up-turned bogie frames are now receiving undercoat now that the frames have been proved defect free. 19 April 2017
Photograph: Darrin Crone.

Inside up-turned bogie frames

The bogie axleboxes have been dye penetrant inspected to ensure there is no cracking in the corners of the flanges that control the lateral position of the axlebox and wheelset. 19 April 2017
Photograph: Darrin Crone.

The bogie axleboxes

The manifold that normally sits inside the cab on top of the firebox and supplies steam to various systems on the locomotive under the control of the crew. The flanges are normally coupled to valves. The manifold has been cleaned and some of the damaged mounting studs have been removed and will be replaced with new. 20 April 2017
Photograph: Darrin Crone.

The manifold

The piston from one of the vacuum cylinders sees daylight infrequently. Dated 1953 it looks to be in as new condition. 20 April 2017
Photograph: Darrin Crone.

A vacuum cylinder piston

The bogie frames by the end of the week covered in undercoat. This will be glossed next but painting of the outside frames and upper surfaces will be completed when the frames are returned to their right way up. This is a view from the front of the bogie. The brackets on the front of the bogie support a beam on which is mounted the AWS receiver. 20 April 2017
Photograph: Darrin Crone.

The bogie frames in undercoat

A view of the painting bench with the bogie side control springs in bright red, ready to refit in the bogie. In the foreground one of the oil boxes which has received it's last attention before fitting to the loco. 20 April 2017
Photograph: Darrin Crone.

Bogie side control springs

The boring of the front top cylinder flanges continued this week with the uppermost in the photograph just bored through. This is the right hand side. Just one more to do each side then this marathon is over. 20 April 2017
Photograph: Darrin Crone.

The front top cylinder flanges

The large oil boxes located just to the rear of the saddle were refitted this week over the recently fitted footplate rivets and newly painted footplating. 21 April 2017
Photograph: Andy Barwick.

The large oil boxes

16 April 2017

New linings were fitted to the reverser clutch this week. This involved heating them in an oven to make them pliable then bending them to the correct curve to fit in the recesses in the clutch. The linings are screwed in place and the screws were replaced as it apears some of the old screws were not of the correct thread type so were found to be damaged upon removal. The complete clutch was then assembled on the bench and the reverser shaft sheaves were used to test the fit. The linings certainly get a good grip.

The overhaul of boiler fittings and valves continued this week with the blower valve striped and inspected. The valve seat lapping was completed and the valve repacked and reassembled. The valve is now ready for reuse. Work has now started on the overhaul of the manifold valves. Some see very little use in traffic, such as the shut off valve for the boiler pressure gauge, however others, such as the steam heat valve don't live such a quiet life and the wear is considerable. Upon inspection of this valve it apears to be life expired and will require replacement.

The new stud for the displaced thrust in the right driving axlebox was made and fitted this week. All the axleboxes are now ready for re-metaling, though we still await the dimensions of the finished journals.

The painters have been busy again with the first primer coats being applied to the inside of the saddle, after a final coat of the needle gun. The Painting Team have been itching to get it painted for weeks.

Inspection of the bogie continued this week with the examination of the front and rear stretchers and all around the horns. The outside central sections of the frame plates are all that remains to be done. By the end of the week the first coat of primer was applied to the underside.

The overhaul of the vacuum brake cylinders began this week with their dismantling. There are three in total, two smaller ones mounted side by side toward the front of the loco with the larger one mounted further back between the frames. The brake hangers and cross beams were mounted on the loco by the 007 Gang of junior volunteers last week, and this week the inspection of these components began.

The outside cylinder bolt hole refurbishment continued this week. Only three remain to be done, all others having now being bored and finish reamed. The jig used so far to ensure accurate alignment will now require modification to access the remaining holes.

Inspection and assessment of the loco draw gear continued this week with the removal of the tender eyebolt and its rubber spring. The eyebolt passes through the front tender dragbox and the intermediate main drawbar is pinned in to it. This has now been measured and its current dimensions will be compared to drawing and permissible wear limits. It can then be decided if it requires any repairs or replacement. Measurement of the front drawhook shows it to be fit for further use, in fact it is surprising how little wear there is on the hook, however until the last ten years, it spent most of its time on the mainline so the front hook probably didn't get much use.

The right hand leading combined brake shaft and spring bracket returned from repair this week. It was trial fitted to the frames on Saturday. Measurements were taken of the trial position and compared to the position of the existing left hand side. As to be expected from a hand built 1930s locomotive that has seen a long active life things are not exactly to drawing so a certain amount of fitting is still required before finally locating the bracket. A cutter has been obtained and a set up devised that will accurately drill mounting holes in the bracket to match the holes already in the frames.

The final rivets were put in to the right hand footplating this week. The last ones went into the slide bar bracket. Attention then turned to putting in the last rivet in the left hand side footplate bracket. Shortly after completing the riveting of the outside slidebar brackets the footplating received its first coats of primer in preparation of refitting the oilbox brackets that sit on the footplate in this area.

The assembled reverser vacuum clutch with new linings in place tested with the reverser shaft sheaves in place. 12 April 2017
Photograph: Darrin Crone.

Reverser vacuum clutch

The upturned bogie frames have been extensively tested to ensure they are free from damage and defects. 12 April 2017
Photograph: Darrin Crone.

Upturned bogie frames

A tiny detail, but requiring making from scratch, a new locating stud has been fitted to the thrust insert in the right driving axlebox. 13 April 2017
Photograph: Darrin Crone.

New locating stud

Not mentioned in the report, the plates at the back of the bufferhead that compress the smaller rubber springs an the back of the buffer assembly have been skimmed to remove deformation from decades of use. 15 April 2017
Photograph: Darrin Crone.

Back of the bufferhead

The tender eyebolt mentioned in this week's report has been examined. 15 April 2017
Photograph: Darrin Crone.

Tender eyebolt

The loco vacuum brake cylinder overhaul has begun. The larger cylinder nearest the camera is mounted between the driving and trailing coupled wheels and the 2 smaller cylinders are mounted in front of the leading coupled wheels. They are linked on the loco by brakegear that combines their brake force. 15 April 2017
Photograph: Darrin Crone.

Loco vacuum brake cylinder

The refurbished combined spring and brake shaft bracket trial fitted to the frames. 15 April 2017
Photograph: Richard Swales.

Refurbished bracket

9 April 2017

The installation of the coupled wheel horn lubricating pipes was completed this week. The trailing set were fitted last week. The remaining mechanical lubricator bleed valves were also cleaned, inspected and refitted this week. While between the frames the combined control reservoir and the air pump exhaust silencer box were also refitted. The tee that splits the steam supply to the steam sands to both sides of the loco has also been fitted.

The overhaul of boiler fittings and valves continued this week with the retrieval from store of the blower valve and the valve that was used to isolate the steam chest pressure signal to the exhaust steam injector, when that was fitted, but is now used to isolate the steam chest pressure gauge. The blower valve was dismantled and the valve was skimmed to return it to its correct profile. The seat was then ground but there are still a couple of marks that will have to be removed. The steam chest isolation valve does not see much operation so was in good condition. When lapped with a little fine abrasive paste it almost immediately showed continuous contact.

The last remaining corners behind the front bufferbeam were needle gunned and primed this week, leaving just the area around the Cartazzi and the bogie stretcher to do. Alan had previously finished stripping and descaling the underside of the bogie and this week its detailed inspection began. The bogie centre casting was di-pen inspected this week. The bogie frame rivets and fitted bolts were also examined and all have proved to be tight.

This week representatives of the Engineering Team visited Llangollen to see progress with the boiler. As reported previously the left hand side out wrapper sheet has be welded in place and work continues on its fitting to the outer door plate and foundation ring. Work has begun on the removal of the combustion chamber stays on both sides, and there is a plasma cutter on site and it is now being used for the removal of the copper tubeplate. The new copper tubeplate being supplied by Crewe is now being machined so we are expecting completion of this in the next couple of weeks.

The inspection and measurement of the loco drawgear continued this week with the front draw hook and coupling shackle. The tender "eyebolt" that the intermediate draw bar is pinned into is the only remaining item that requires inspection but first we have to find a spanner to fit the large nut that fastens it in place.

We had another riveting session on Friday and the team got on very well. Unfortunately the old rivets on the leading left hand footplate bracket had come loose over last weekend, due to the clamping of the new rivets we put in. So these had to be removed and new rivets put in. By the end of the day all the left hand footplating had been riveted, except for one hole. When inspected the next day all were tight. We are still trying to work out how to get a rivet in to this last hole.

On Saturday the 007 Gang, our Junior Volunteers, retrieved the brake hangers and beams from store and refitted them to the loco. They did very well to refit these heavy parts on the loco. They have been refitted as we plan to measure their positions prior to refurbishment. After they completed this task they then started to descale under the tender front dragbox.

The boring and reaming of the outside cylinder holes is going well with more that half the holes bored and approximately half the holes finish reamed. A number of bolts are life expired where the saddle casting and middle cylinder are fastened together. On Saturday we began the process of replacement by drilling and then punching out the first two.

A view of the original copper tubeplate. The combustion chamber side stays have had their heads removed and are being drilled out.
Photograph: Trevor Camp/SNGLT.

The original copper tubeplate

The rear top side corner stays are also being renewed at this overhaul. This picture show the right hand side.
Photograph: Trevor Camp/SNGLT.

The rear top side corner stays

The partially assembled air pump awaits the return of the repaired steam cylinder at the back left of the bench. Not mentioned in the report, new stainless steel springs were fitted to the air pump non return valves this week. The primed components are parts of the reverser vacuum clutch.
Photograph: Peter Brackstone.

The partially assembled air pump

The refitted air pump exhaust box sits on the steam sand box to the right of the picture. The taped up fitting on the horizontal stretcher is the tee to the steam sands supply.
Photograph: Peter Brackstone.

Refitted air pump exhaust box

The bogie centre has been thoroughly cleaned and is being inspected by Bob Shearman.
Photograph: Darrin Crone.

The bogie centre cleaned

A corner section of the bogie centre casting. The bogie is upside down so the bottom of the bogie is at the top of the picture and the rivet heads secure the casting to the left hand bogie frame plate. It can be seen that the corners have been extended to give the frame plate extra support. Existing rivet holes were welded up and new rivets put in when the corners were extended. The new sections are marked on their edge 2553.
Photograph: Darrin Crone.

Corner section bogie centre

The horn lubrication pipes are now all installed.
Photograph: Darrin Crone.

The horn lubrication pipes

Two new rivets put in the left hand slide bar bracket. The corner hole apears never to have been riveted as the footplating above has never been drilled through.
Photograph: Darrin Crone.

Two new rivets

The brake hangers and beams have been fitted so that they can be dimensionally checked prior to refurbishment.
Photograph: Darrin Crone.

The brake hangers and beams

2 April 2017

The brass oil boxes for lubricating the coupled wheel horns were fitted last week and the oil pipes were retrieved from store and cleaned. This week they were annealed and then the set for the trailing set of horns fitted. The remainder are ready to install. Also this week the bleed valves that are in the lubricating lines from the mechanical lubricator to the coupled wheel under keeps were were also retrieved from store. They were dismantled and cleaned out and all apear in good condition. A start was made on fitting them on their brackets at the top of the frames.

The combined control reservoir that, with the DV2 valve, allows vacuum brake application to be controlled when the loco is operating an air braked train was retrieved from store this week. It was pressure tested and examined and will be suitable for further use. By the end of the week it had been repainted and is now ready for refitting. A lot of time was spent last week painting the numerous individual small brackets between the frames that clamp pipework in position. Fitting the lubrication clips that are fastened under the splasher frame bracket bolts was completed this week.

The coupled wheel axleboxes have bronze thrusts on the horizontal diameters. These are kept in place by headless screws, however one screw is missing and the thrust has moved slightly. This was carefully repositioned and the thread cleaned up. A new screw will be made and fitted.

The inspection of the intermediate drawgear continued this week, with the main drawbar being measured and compared to the LNER/BR drawing and the permissible wear allowances. The loco drawbar pins, main and safety link, also received this attention.

The reassembly of the air pump started this week. It cannot be completed yet as we are waiting for the return of the steam cylinder and new springs for the non-return valves. The Air Pump refurbishment team have now turned their attention to the reversing shaft vacuum clutch. This clamps tight to the reversing shaft to secure the valve gear cut off position. The clutch has now been stripped and inspected. The clutch operates through the application of vacuum on a rubber diaphragm and this diaphragm will be replaced. The grip on the shaft is achieved with brake linings, and these also require replacement. One interesting find was the marking on the clutch of 2510 and 15, both numbers carried by A4 60015 Quicksilver.

The needle gunning of the upturned bogie was completed this week. The bottom of the bogie structure can now be di-pen NDT examined.

Last week the hole for a new fitted bolt was prepared on the right leading coupled wheel horn and this week the new bolt was machined and fitted. Work on the repair of the cylinder flange holes continued with some holes bored and another completed by reaming through.

We finally got back on to riveting this week with both front footplate sections being riveted on to the brackets over the 2 to 1 link cut outs. The right hand side required four out of five rivets replacing whereas the left required two replacing.

On Friday the combined spring and brake bracket was receiving its last attention at the works of K D Flavell with the groove for the Spenser spring box being cut. At Buckfastleigh all the coupled wheel tyres have now been finished profiled and journals and thrust faces are now being measured and skimmed where required.

The combined control reservoir was manufactured by BR at Crewe in 1972 and feels like it is made from armour plate. 29 March 2017
Photograph: Darrin Crone.

Combined control reservoir

The trailing pair of horn lubricating brass oil boxes were fitted last week. This week the oil pipes were installed. At the top of the frames near the oil boxes are small bleed valves on brackets that are in the lubrication lines from the mechanical lubricators to axlebox underkeeps. 30 March 2017
Photograph: Darrin Crone.

Horn lubricating brass oil boxes

The outer strap of the vacuum clutch bears marking 15, 2510 and 7, with 15 and 2510 struck through. 30 March 2017
Photograph: Darrin Crone.

Outer strap of vacuum clutch

The complete vacuum clutch and the split sheave that clamps on to the reversing shaft. The gap between the sheeve and the outer strap of the vacuum clutch housed a brake lining removed in the photo. The clutch is mounted horizontally on the face that it sits on the bench in the photo. 30 March 2017
Photograph: Darrin Crone.

Vacuum clutch & split sheave

The new left hand outer wrapper side sheet is now being installed. 30 March 2017
Photograph: Peter Brackstone.

New outer wrapper side sheet

The whistle was refitted this week for sounding on the 50th anniversary of the loco's first run in preservation. 31 March 2017
Photograph: Peter Brackstone.

Whistle refitted

New rivets fitted to the front right footplate bracket. 1 April 2017
Photograph: Darrin Crone.

New rivets fitted
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